Showing posts with label Civil Failure. Show all posts
Showing posts with label Civil Failure. Show all posts

Monday, 11 June 2012

Civil Failure


Thursday, 7 June 2012

Failure Analysis Of Mishap At DMRC On 12 July


It was 12th July 2009 which proved to be the darkest day in the history of DMRC. After achieving a milestone of providing a reliable and easy mean of transportation to the capital of India, it is now facing huge problems which are not only causing loss of human lives but also causing immense damage to the most reputed infrastructure organization of India. So far, this company has achieved every target ahead of schedule under the excellent guidance of Mr. Sreedharan.
Let us try understanding what went wrong on that disastrous day
On 12th July, 2009, while lifting segments of the superstructure, an accident happened in the Badarpur – Secretariat section near P-67. The pier cap of pier P-67 got collapsed causing subsequent collapse of the
(i) Launching Girder
(ii) Span between P-66 and P-67 which had got erected and pre-stressed, already
(iii) Segments of the superstructure for the span between P-67 and P-68.
The incident left 6 people dead and many injured.
Site Investigation
After visiting the site, following observations were noticed
1. The pier cap of affected pier (P-67) has sheared from the connection point of the pier and pier
cap. It is a cantilever pier cap. It was informed by the contractor and DMRC representatives that the support system for viaductwas initially designed as portal pier till the casting of the pier was over. The shop owners put up resistance against casting of the other leg of the portal and it was subsequently decided by DMRC that this would be changed to a cantilever pier, similar to P-68 which is still standing at site.
metro collapse Pier fall
2. It was noticed that the prop support of the cantilever has failed from its connection to the pier.
3. The top reinforcement of the cantilever beam does not have any development length into pier
concrete. As learned from the sources, the top reinforcement of the cantilever beam had an “L”
bend of 500 mm only.
p67-p68fall
There is very nominal (or no trace) of shear reinforcement at the juncture.
4. The launching girder has fallen below with the failure of pier cap. Also, the span between P-67
and P-68 has fallen inclined, supported by the ground at one end and pier cap (P-68) on the
other.
top-reinforcement
5. The boom of the crane, used for lifting the launching girder on 13 July, 2009, has failed in bending
and shows clear sign of overloading.
overloaded-crane-crash
Analysis 
i. The pier (P-67) was initially designed as a leg of a portal frame and subsequently changed to support cantilever pier cap.
ii. The same method was followed for P-68 and P-66.
iii. The alignment of track here is in curvature and gradually leaves the median of the road to align on one side of the road.
iv. The longitudinal reinforcement of the pier was protruding by around 1500 mm beyond top of pier.
v. The top reinforcement of pier cap was 36 mm in diameter and had a development length of 500 mm. only as an “L” from the top. There was insufficient bond length for the structure to behave like a cantilever beam.
vi. During launching operation of the launching girder itself, this pier cap developed crack and work was stopped for couple of months. During this period, the cantilever pier cap was grouted in crack areas and further strengthened by introducing prop or jacketing.
vii. However, the behavior of the structure changed due to introduction of this jacket and the cantilever pier cap remained no more cantilever.
viii. The segments of superstructure for the span between P-66 and P-67 was erected and launched and the prop beam / jacketing could sustain the load to that extend.
ix. During the launching of superstructure segments between P-67 and P-68, only 6 segments could be lifted and the whole system collapsed when seventh segment was hooked for lifting.
The sequence of failure is as follows:
a. The support of the prop / jacket got sheared from its connection due to inadequate section / welding.
b. The cantilever pier cap which was behaving as a simply supported beam due to introduction of prop / jacket started behaving like a cantilever beam suddenly after failure of the prop which it can not sustain ( It was inadequately designed). So, the so called “cantilever pier cap” collapsed.
c. The launching girder / span between P-67 & P-66 / the temporarily erected segments between P-67 and P-68, all got collapsed in one go.
Crane Failure
The launching girder was lifted by the cranes. However, it needed to be pushed little forward for
unloading it on the ground. So, all the cranes were asked to stretch there booms by some length.
During this operation, the 250 MT capacity crane on extreme left exceeded it’s capacity and the
boom failed and broke down. Since, there were unequal loading on the 250 MT crane by it’s side,
that also failed and broke down. The crane of 350 MT capacity didn’t broke but it toppled with it’s
base. The 400 MT crane remained intact.
Final overview 
a. It is concluded that the failure of pier cap occurred due to inadequate prop / jacket. This was coupled with failure of cantilever pier cap due to inadequate development length of top reinforcement of the cantilever pier cap.
b. The failure of the crane was a case of operational inexperience for such synchronized crane operation. The crane -1 did not have the requisite capacity for the extended boom length and radius. Once crane – 1 failed, the crane – 2 was loaded almost half of the launching girder amounting to around 200 MT. For the extension of boom and radius, it did not have the requisite capacity so it failed, too. The crane -3 was loaded more than it’s capacity. However, in this case the crane got toppled instead of boom getting sheared. The crane -4 did not undergo the severe loading due to failure of other 3 cranes and most of the loads got grounded by that time.
What it taught us?
a. Structural designs should be proof checked by experienced structural engineer.
b. Once failure observed, structure should be as far as practicable abandoned and new structure should be built up
c. More emphasis should be given on detailing of reinforcement to cater for connections and behavior of the structural components.
d. Any make-shift arrangement to save a failed structure should be avoided.
e. Reinforcement detailing in corbels, deep beams, cantilever structures should be checked as per the provisions of more than one type of Standards (both IS & BS should be followed).
f. Adequately experienced Engineer / Forman should be deployed for erection works.

Minneapolis I-35W Bridge Collapse – Engineering Evaluations and Finite Element Analysis

Abstract
The National Transportation Safety Board (NTSB) investigates accidents to identify the probable cause and to make recommendations that would prevent similar accidents. Following the collapse of the I-35W bridge in Minneapolis on August 1, 2007, the NTSB worked with the Federal Highway Administration, the Minnesota Department of Transportation and other parties with information and expertise, including SIMULIA Central, to determine the circumstances that contributed to the collapse of the bridge, completing the investigation in 15 months. The NTSB concluded that the collapse of the bridge was caused by the inadequate load capacity of gusset plates used to connect the truss members, as a result of an error by the bridge design firm, Sver-drup & Parcel and Associates, Inc. The loading conditions included a combination of (1) substantial increases in the weight of the bridge caused by previous bridge modifications, and (2) the traffic and concentrated construction loads on the bridge on the day of the collapse. Evidence from the collapsed bridge structure, engineering evaluations of the design, and results from the finite element analyses used to support the investigation are reviewed.
Keywords: Bridge Collapse, Gusset Plate, Plasticity, Instability, Riks, Fasteners.
Introduction
About 6:05 p.m. central daylight time on Wednesday, August 1, 2007, the eight-lane, 1,907-foot-long I-35W highway bridge over the Mississippi River in Minneapolis, Minnesota, experienced a catastrophic failure in the central deck truss span over the river. The 1,064-foot-long deck truss portion of the bridgecollapsed, along with adjacent sections of the approach spans that were supported by the deck truss. See Figure 1. A total of 190 people were confirmed to have been on or near the bridge when the collapse occurred; 13 people died, and 145 people were injured. There were 111 vehicles on the portion of the bridge that collapsed, with 17 recovered from the water.
The collapsed deck truss portion of the I-35W bridge.
The National Transportation Safety Board (NTSB) launched a team of investigators to the accident scene, with on-scene work beginning on the day after the collapse. The on-scene investigation, including documentation and analysis of the recovered bridge structure, lasted until November 10, 2007. The results of the investigation were presented in the NTSB’s final report [NTSB 2008k], which was adopted on November 14, 2008.
The NTSB is an independent federal agency charged with investigating all aviation accidents in the United States and investigating major accidents involving highways, railroads, pipelines, hazardous materials and marine transportation. The goals of every investigation are to determine the probable cause of the accident and to make recommendations for systemic changes that would prevent similar accidents.
In order to accomplish its mission, the NTSB collaborates with parties involved in the accident who have specialized technical knowledge or expertise that can contribute to the investigation. For the collapse of the I-35W bridge, the parties to the investigation included the Federal Highway Administration (FHWA); the Minnesota Department of Transportation (Mn/DOT) and their consultant Wiss, Janney, Elstner Associates, Inc. (WJE); Jacobs Engineering Group, Inc. (Jacobs), which purchased Sverdrup Corporation (successor to the original bridge design firm) in 1999; and Progressive Contractors, Inc. (PCI), which was repaving part of the deck on the day of the accident.
Bridge design 
The I-35W bridge was designed by the engineering consulting firm of Sverdrup & Parcel and Associates, Inc., of St. Louis, Missouri. The design was based on the 1961 American Association of State Highway Officials (AASHO) Standard Specifications for Highway Bridges and 1961 and 1962 Interim Specifications, and on the 1964 Minnesota Highway Department Standard Specifications for Highway Construction. The bridge design was developed over several years. Plans for the foundation were approved in 1964 and construction of some piers began in 1964. The final design plans for the bridge were certified by the Sverdrup & Parcel project manager (a registered professional engineer) on March 4, 1965. The bridge design plans were approved by the Minnesota Highway Department on June 18, 1965.
Bridge construction 
The bridge was 1,907 feet long and carried eight lanes of traffic, four northbound and four southbound. The bridge had 13 reinforced concrete piers and 14 spans, numbered south to north. Eleven of the 14 spans were approach spans to the deck truss portion. The bridge deck in the approach spans either was supported by continuous welded steel plate girders or by continuous voided slab concrete spans. The south approach spans were supported by the south abutment; by piers 1, 2, 3, and 4; and by the south end of the deck truss portion. The north approach spans were supported by the north abutment; by piers 9, 10, 11, 12, and 13; and by the north end of the deck truss portion. The 1,064-foot-long deck truss portion of the bridge encompassed a portion of span 5; all of spans 6, 7, and 8; and a portion of span 9. The deck truss was supported by four piers (piers 5, 6, 7, and 8).
The original bridge design accounted for thermal expansion using a combination of fixed and expansion bearings for the bridge/pier interfaces. The fixed bearing assemblies were located at piers 1, 3, 7, 9, 12, and 13. Expansion (sliding) bearings were used at the south and north abutments and at piers 2, 4, 10, and 11. Expansion roller bearings were used at piers 5, 6, and 8.
The deck of the I-35W bridge consisted of two reinforced concrete deck slabs separated by about 6 inches. The total width of the deck slabs was about 113 feet 4 inches. When the bridge was opened to traffic in 1967, the cast-in-place concrete deck slab had a minimum thickness of 6.5 inches. As discussed later in this report, bridge renovation projects eventually increased the average thickness of the concrete deck by about 2 inches.
Deck truss portion of the bridge 
In a deck truss bridge, the roadbed is along the top of the truss structure. The deck truss portion of the bridge consisted of two parallel main Warren-type trusses (east and west) with verticals. A Warren truss has alternating tension and compression diagonals and has the advantage that chord members are continuous across two panels, with the same force carried across both panels. This arrangement simplifies some of the design calculations.
The upper and lower chords of the main trusses extended the length of the deck truss portion of the bridge and were connected by straight vertical and (except at each end of the deck truss) diagonal members that made up the truss structure. The upper and lower chords were welded box members, as were those diagonals and verticals that were designed primarily for compression. The vertical and diagonal members designed primarily for tension were H members consisting of flanges welded to a web plate.
Gusset plates were used to connect the truss members. The gusset plates were primarily attached to the truss members with rivets, but a few bolts were used at each joint, presumably to expedite the initial connection during construction.
The east and west main trusses were spaced 72 feet 4 inches apart. The deck was supported by 27 transverse welded floor trusses spaced on 38-foot centers along the main trusses and by two floor beams at the north and south ends. The floor trusses were cantilevered out about 16 feet on either side past the east and west main trusses. The concrete deck for the roadway rested on 27-inch-deep wide-flange longitudinal stringers attached to the transverse floor trusses and spaced on 8-foot-1-inch centers. The 14 stringers were continuous for the length of the deck truss except for five expansion joints. Diaphragms connected the webs of adjacent stringers to transfer lateral loads and maintain structural rigidity and geometry.
The main truss nodes were numbered from the south beginning from 0, reaching node 14 at the center of the deck truss above the river. Because the bridge was nearly symmetric north to south, the nodes on the north end of the bridge were numbered in reverse order and given a prime symbol, so that U10 and U10? indicate symmetric nodes with respect to the center of the deck truss. The letters U (for upper chord) and L (for lower chord) further identified the nodes, along with E or W to specify the east or west main truss.
These node numbers were also used to identify the connecting main truss structural members. For example, the upper chord member that connected the U9 node to the U10 node was designated U9/U10 (or U10/U9). Again, E and W were used to designate the east or west main truss.
For the most part, forces were only transferred between truss members at the nodes where the diagonals connected to the upper and lower chords. These nodes alternated between the upper and lower chords along the bridge, so that, for example, L9, U10 and L11 are nodes where forces are transmitted. Conversely, the chord members were continuous through nodes U9, L10 and U11, with only a token connection to the verticals for stability, and no forces were intended to be transferred to other members at those nodes. Loads from the transverse floor trusses tied into the verticals at a point between the upper and lower chords. As a result, at U10, the vertical was in tension, while at L9 or L11, the vertical was in compression.
The deck truss portion of the bridge was also stiffened by sway braces at each panel point below the floor trusses, and by angled lateral braces extending between panel points.
Bridge history 
The bridge was opened to traffic in 1967. The original dead weight of the deck truss portion of the bridge was estimated to be 18.3 million pounds. Two later modifications to the bridge caused significant increases in the weight of the deck truss portion of the bridge. In 1977, a renovation project involved milling the bridge deck surface to a depth of 1/4 inch and adding a wearing course of 2 inches of low-slump concrete, adding some 3 million pounds to the deck truss portion of the bridge. This project was intended to provide additional protection against corrosion for the steel reinforcing bars in the deck. In 1998, the median barrier and outside railings were upgraded to meet revised standards, adding 1.2 million pounds to the deck truss portion of the bridge.
During the summer of 2007 until the day of the collapse, renovation work was underway to remove the concrete wearing course to a depth of 2 inches and add a new 2-inch-thick concrete overlay. At the time of the bridge collapse, four of the eight travel lanes (the two outside lanes northbound and the two inside lanes southbound) were closed to traffic. The preexisting wearing surface was still in place on the two inside lanes northbound, where the average deck thickness was 8.7 inches. The new overlay was already in place on the two outside northbound lanes (average deck thickness of 8.8 inches) and the two outside southbound lanes (average deck thickness of 8.9 inches). The surface of the two inside southbound lanes had been milled for the entire length of the bridge, removing about 2 inches of material.
On the day of the collapse, aggregates and equipment for the repaving project were staged on the center span of the deck truss portion of the bridge. The construction aggregates were distributed in eight adjacent piles (four truckloads of sand and four of gravel) placed along the median in the leftmost southbound lane just north of pier 6. Along with the aggregates in this area were a water tanker truck with 3,000 gallons of water, a cement tanker, a concrete mixer, one small loader/excavator, and four self-propelled walk-behind or ride-along buggies for moving smaller amounts of materials. The documented delivered weights for the aggregates staged on the bridge were 184,380 pounds of gravel and 198,820 pounds of sand. The estimated weight of the parked construction vehicles, equipment, and personnel in this area was 196,000 pounds. Figure 2 is a photograph showing the sand and gravel piles about 2 hours before the collapse.
The locations and weights of the construction materials and vehicles
Figure-2 The locations and weights of the construction materials and vehicles
A post-accident survey was made to identify all of the vehicles, workers and construction materials on the bridge at the time of the collapse [NTSB 2007]. The locations of the vehicles, workers and materials were determined from witness statements and photogrammetry. Each vehicle was weighed if possible, or the weight estimated from a vehicle database. Weather data was also collected for the area on the day of the collapse.
Findings from the wreckage and the video 
The disposition of the wreckage indicated that the collapse initiated in the central span of the deck truss portion of the bridge, with the structure north and south of the river being pulled toward the river. The bridge components were examined and the damage documented [NTSB 2008b], and the locations of the bridge components and the observed damage were used to identify the sequence of the collapse [NTSB 2008g].
The deck truss portion of the bridge separated into three sections. The separations occurred at symmetric positions north and south of the center of the bridge, through both the east and west trusses. Fractures through the U10 and U10? gusset plates severed the connections of the upper chords and the connections between the L9/U10 and L9?/U10? compression diagonals and the central section of the bridge. The lower chords were severed by fractures through the L9/L10 and L9?/L10? members adjacent to the gusset plates at the L9 and L9? nodes. The positions of the fractures are indicated in Figure 1 and in a pre-collapse photograph in Figure 3.
Figure 3-Identifying the nodes on the west main truss
Evidence from a motion-activated video surveillance camera on the south side of the river indicated that the south end of the bridge began to fall before the north end, so the investigation concentrated on the fractures in the U10 gusset plates and the L9/L10 lower chord members [NTSB 2008e]. The video also showed that the bridge fell without appreciable side-to-side rotation, indicating that the fractures on the east and west trusses occurred nearly simultaneously.
Residual plastic deformation showed that the fractures in the L9/U10 lower chord members adjacent to the L9 nodes occurred under severe bending, which would only have been possible if the truss was already fractured at another location and the opposite ends of the members were free to move. These fractures were therefore not primary, and the focus of the investigation shifted to the U10 gusset plates.
The deformation and fractures in the U10 gusset plates surrounding the upper ends of the L9/U10 compression diagonals were consistent with the in-plane loads expected in the truss. See Figures 4 and 5. The damage was consistent with bending and tearing of the gusset plates under compression above the ends of the L9/U10 diagonals, with fractures under tension through the bottom rows of rivets on the L9/U10 diagonals adjacent to the verticals. These fractures in the U10 gusset plates left a portion of each gusset plate attached to the upper ends of the separated diagonals L9/U10, with a V-shaped piece of each gusset plate extending beyond the ends of the diagonals. On both the east and west diagonals, these V-shaped pieces were bent toward the east, indicating that the upper ends of the diagonals shifted laterally to the west as the gusset plates deformed and fractured, and the east side plates of the diagonals penetrated through the interior structure of the nodes.
Figure 4.  Reconstructed U10W components
Figure 5.  A map of the fractures in the east gusset plate of the U10W node
The loss of structural support from the bending and fracturing of the U10 gusset plates and the lateral shift of the L9/U10 diagonals allowed the remainder of the U10 nodes to drop downward. This downward displacement resulted in bending loads that fractured the gusset plates between the upper chord members. The direction of bending showed that the U10 nodes had dropped below the levels of the U9 and U11 nodes.
The fractures on the north side of the bridge (in the U10? gusset plates and in the L9?/U10? lower chord members) were very similar to the fractures on the south side of the bridge.
Because the fractures and deformations in the U10 gusset plates were consistent with the expected loading in the truss, these gusset plates were likely points of initiation of the collapse, and therefore a primary focus of the investigation. A detailed study of the U10 gusset plates was the initial task undertaken using finite element analysis.
There was no evidence that the U10 gusset plates had any pre-existing cracking (such as from fatigue) or corrosion damage before the bridge collapse, indicating that the gusset plates failed as a result of overloading. It was therefore necessary to compare the loads on the bridge to the capacity of the design.
Review of the design 
The bridge was designed using an Allowable Stress methodology, whereby the stresses arising from specified design loads were required to be less than material-specific allowable stresses. This methodology built in safety both in the specification of the design load and in the allowable stress level. The design loads included the dead load of the weight of the bridge plus a worst-case live load approximating multiple lanes of heavy trucks, and an added 50 percent of the live load to account for dynamic effects (referred to as impact). Under the applied design loads, the stress in each component was required to be less than the allowable stress for that component. This allowable stress would have been no more than 55 percent of the yield stress, depending on the type of load applied (tension, compression, or shear). The allowable stresses for truss members in compression were further decreased to guard against buckling.
Following the bridge collapse, the Safety Board received sets of design documents from both Mn/DOT and Jacobs. In addition to the design drawings, both entities provided identical collections of several hundred pages of sequentially numbered and indexed compilations of checked computation sheets showing calculations performed for the final design of the bridge. The computation sheets for the deck truss superstructure contained design calculations for the welded gusset plates used in the floor trusses, but none of the records from Mn/DOT or Jacobs Engineering showed any calculations for the gusset plates on the main trusses.
Using a basic design methodology consistent with that used by Sverdrup & Parcel to design the gusset plates for the floor trusses, FHWA engineers calculated the stresses on the main truss gusset plates that would be generated by the design loads (demand) in the members secured by the gusset plates [Holt 2008]. Comparing these stresses to the allowable stresses (capacity) in the AASHO specifications resulted in demand-to-capacity (D/C) ratios that illustrate the expected performance of the gusset plates. A D/C ratio of slightly greater than 1 (demand exceeds design capacity) are sometimes acceptable based on the professional judgment of an engineer. A D/C ratio significantly greater than 1 likely indicates a design error.
Figure 6.  Calculating the gusset plate shear stress on a horizontal section from the design loads indicated
The evaluations considered stresses on two critical sections in each gusset plate – one horizontal section near the center of the gusset along the edge of the chord members, as shown in Figure 6, and one vertical section adjacent to the vertical member of the node. Results of the horizontal section calculations are provided in Figure 7, showing that the gusset plates at the U4, U10, and L11 nodes had D/C ratios for shear that exceeded 2. In addition, the gusset plates at two other nodes had D/C ratios slightly over 1 for shear. The analysis indicates that the gusset plates at the U4, U10, and L11 nodes were only half as thick as necessary to meet the design requirements.
Figure 7.  D/C ratios for the gusset plates along the truss, shown with a sketch of the south end of the bridge.
Lines of corrosion were found on the L11 gusset plates along the upper edges of the lower chord members. The L11 gusset plates were fractured at or near the lines of corrosion, separating the vertical and diagonals from the lower chord members. The gusset plates were intact along the lower chord members, maintaining continuity along the lower chord through the node. Because the stress evaluation showed that the L11 gusset plates were only about half as thick as required, there was concern that the inadequate gusset plate thickness coupled with the corrosion might have played a role in the collapse. A detailed study of the gusset plates at the L11 nodes with corrosion was therefore an additional task undertaken using finite element analysis.
Finite element analysis 
The NTSB formed a group to perform finite element analyses in support of the investigation. In addition to participation in the group by parties to the investigation, the NTSB acquired added expertise and resources through an external contract with the State University of New York at Stony Brook and a subcontract with the Central Office of Dassault Systemes SIMULIA Corporation (SIMULIA Central). All of the analyses were performed using Abaqus/Standard. A parallel investigation was undertaken by the Federal Highway Administration Turner-Fairbank Highway Research Center (TFHRC) in collaboration with this effort, and the investigation relied heavily on global models of the bridge that were constructed at the FHWA TFHRC. Details of the analyses are provided in several reports [Ocel 2008, NTSB 2008c, NTSB 2008j].
Information gained from examining the wreckage was used to guide the modeling effort and evaluate results. Based on findings from the accident scene, the modeling was initially focused on the U10 nodes. The modeling effort was expanded to include the L11 nodes as a result of the FHWA’s gusset plate adequacy analysis, which showed that the gusset plates at both the U10 and L11 nodes had inadequate load capacity, coupled with the fact that the L11 gusset plates were found to have areas of corrosion, which further reduced their load-carrying capacity.
Inputs to the modeling effort 
The models were based on the original Sverdrup & Parcel design plans and the Allied Structural Steel shop drawings. The FHWA developed a three-dimensional global model of the entire deck truss portion of the bridge, constructed with beam and shell elements. See Figure 8. In addition, both the FHWA and SUNY/SIMULIA created detailed models of the U10 and L11 nodes to examine the fine details of stress distribution. These detailed models were built into the FHWA global model of the bridge. See Figure 9. The FHWA detailed model generally used shell-element representations for the truss members and the gusset plates, while the SUNY/SIMULIA detailed models used solid-element representations; the solid-element approach was in part motivated by a goal of considering stress concentrations associated with the riveted connections.
Figure 8.  The FHWA global model consisting of beam and shell elements.
Figure 9.  U10W and L11W detailed models built into the FHWA global model
The boundary conditions at the piers for the global model were calibrated using live load strain gauge data obtained by the University of Minnesota as part of a 1999 fatigue assessment of the I-35W bridge. The data fell between results from a model with fixed bearings and a model with free bearings. Good agreement was obtained with a model using fixed bearings, but including flexibility in the concrete piers. The approach spans supported at each end of the deck truss portion of the bridge were replaced with spring elements.
Loads were applied in steps to mimic the history of the bridge. The original weight of the as-built bridge was calculated by the FHWA from a careful audit of the steel called out in the shop drawings. The thickness of the deck in different areas of the bridge was based on cores taken after the accident. In the initial load step, the weight of the concrete was applied using forces only to model wet concrete. In the next load step, the concrete forces were replaced with shell elements to model the hardened concrete. Subsequent load steps included the increase in weight associated with the 1977 increase in deck thickness, the increase in weight associated with the 1998 change in the median barrier and outside railings, and the decrease in weight associated with the removal of part of the deck in the repaving operation that was underway at the time of the collapse. The final load steps introduced the traffic and the construction loads on the bridge at the time of the accident [NTSB 2007].
Photographs from 1999 and 2003 were used by NTSB to estimate the magnitude and direction of bowing distortion in the U10W and U10E gusset plates for input to the models [NTSB 2008f]. See Figure 10. The bowing distortion was included as an initial imperfection. The estimate of the maximum bowing magnitude used for input to the models was 0.60 ± 0.15 inch. To generate bowing consistent with that shown in the photographs, it was necessary to use an initial maximum deflection of 0.5 inch in the unloaded model, which increased to 0.6–0.7 inch after application of the original bridge dead load plus the added deck and the modified barriers (the loading condition at the time the bowed gusset plates were photographed).
Figure 10. Gusset plate bowing distortion at one of the U10 nodes
Measurements of the loss of thickness in the L11 gusset plates were made using a point micrometer and with a laser scanner attached to a coordinate-measuring-machine arm [NTSB 2008h]. The measurements from the four different gusset plates (two each at L11E and L11W) were averaged and incorporated in the models as a strip of reduced thickness in the gusset plates along the upper edges of the chord members being connected.
Gusset plate material properties were based on tensile tests performed by the FHWA on samples from undamaged areas of the four U10E and U10W gusset plates [Beshah 2008]. The measured yield stresses of all of the tensile test samples exceeded the final design plan specified minimum tensile yield stress of 50 ksi. Rivet properties were estimated from hardness measurements performed by the NTSB [NTSB 2008a, NTSB 2008d].
Selected results from the modeling effort 
The models showed that the U10 gusset plates were loaded beyond their yield stress under the dead weight of the as-built 1967 bridge (Figure 11). At that stage of loading, the areas of yielding were confined to a small area above the ends of the L9/U10 compression diagonals. As the weight of the bridge was increased by the 1977 and 1998 modifications, the areas above the yield stress expanded around the ends of the L9/U10 compression diagonals, and the areas above the ends of the U10/L11 tension diagonals began to yield as well (Figure 12). Under the added weight of the traffic and construction materials and vehicles on the day of the accident, almost all of the U10 gusset plates surrounding the upper end of the L9/U10 compression diagonal were yielding (Figure 13). Because the construction materials were staged on the west side of the bridge, the U10W gusset plates were yielding to a greater extent than those at U10E, with instability therefore occurring first at U10W.
Figure 11-Mises stress contours under the dead load of the original 1967 bridge
The yielding of the U10W gusset plates surrounding the upper end of the L9/U10W compression diagonal created a plastic hinge in the structure, and the finite element analysis indicated that the collapse initiated by a local bending instability in the U10W gusset plates. This instability allowed for a lateral shift of the upper end of the L9/U10W diagonal, as indicated in Figure 14, removing support from the central portion of the bridge.
The bending instability in the gusset plates first manifested itself as a failure to converge under increasing load. The instability was further studied and confirmed as a structural instability using Riks analysis and using an applied displacement approach. In the applied displacement approach, the displacement increment associated with a small load increment just before the onset of instability was calculated, and that displacement increment was extrapolated and used as a boundary condition. In the Riks analysis and the applied displacement approach, the bending of the gusset plates and lateral shift of the upper end of the L9/U10 diagonal was shown to increase under decreasing load.
The majority of the analyses used simplified Abaqus fasteners to model the riveted connections. Stress concentrations associated with rivets were investigated using submodels with detailed three dimensional models of the rivets in the most highly stressed areas. These models indicated that no material failure would be expected in the gusset plates before the onset of instability.
Figure 12-Mises stress contours after the 1977 and 1998 modifications.
Figure 13-Mises stress contours under the estimated loads on the bridge at the time of the collapse.
Figure 14-Indicating the lateral shift of the L9/U10W diagonal, with Mises stress contours
Beyond the point of instability, the Riks analysis and the applied displacement approach showed that the deformation in the gusset plates would reach levels where material failure would be expected. Peak stresses and strains appeared in locations consistent with the fractures observed in the post-accident examination of the wreckage.
The design loads for the five truss members that joined at U10W are shown in Table 1. The loads in those members over the history of the bridge are shown in Figure 15. The figure shows that the members were at the most about 5 percent above their design loads under the best estimate of the conditions on the bridge at the time of the collapse. The intent of the design methodology should have ensured that, under the design load, the stress in the gusset plates would have been no more than 55 percent of the yield stress. The yielding in the gusset plates under only the dead weight of the original 1967 bridge confirms the inadequate thickness of the gusset plates identified in the FHWA design review.
U9/U10L9/U10U10/L10U10/L11U10/U11
Design load (kips)2,1472,2885401,975924
ModeTensionCompressionTensionTensionCompression
Figure 15 also shows that the concentration of the construction materials and vehicles above U10W increased the loads in the members significantly, but the most highly loaded member (L9/U10) was estimated to be only about 5 percent above its design load. Properly designed gusset plates should still have has a significant margin of safety under these loading conditions. Also, the increase in load arising from the construction materials and vehicles was similar to that associated with the 1977 increase in deck thickness. Thus, it was concluded that the concentrated stockpiling of construction materials and vehicles on the bridge could not be identified as the sole cause of the collapse. The increases in load over the history of the bridge were part of the circumstances that triggered the collapse, but they would not have been sufficient to cause the collapse if the main truss gusset plates had met their design requirements.
Figure 15.  Loads in the five truss members connected at U10W over the history of the bridge.
In order to trigger the instability, it was necessary to increase the loads above the best estimate of the loads on the bridge at the time of the collapse, as indicated by the two failure cases shown in Figure 15. In one case, only the construction loads were increased, while in the second case, all of the loads were increased. Figure 15 shows that the load in the L9/U10W necessary to trigger failure was the same in both cases, about 5 percent higher than the L9/U10W load under the best estimate of the collapse loads. Comparing the two failure cases showed that the instability was triggered at a critical value of the load in the L9/U10W diagonal and a critical magnitude of the out-of-plane bending displacement of the gusset plates. Figure 16 shows this result clearly for the two failure cases (labeled A1 and A2 in the figure). Figure 16 plots both the load in the L9/U10W diagonal and the total load on the bridge as functions of the lateral displacement on a point on the outside U10W gusset plate. The load in the L9/U10W diagonal and the displacement follow nearly identical paths for the two failure cases considered, even though the total loads on the bridge are significantly different.
Including the photographically documented bowing distortion of the U10W gusset plates in the model reduced the load required to trigger instability and changed the direction of the deformation. With the U10W gusset plates bowed in the directions shown in the photographs, the upper end of the L9/U10W diagonal shifts to the outside of the bridge at instability, consistent with the direction that the diagonal was observed to have shifted by the examination of the collapsed bridge structure. With initially flat U10W gusset plates in the model, the upper end of the L9/U10W diagonal shifted toward the inside of the bridge at instability, which is not consistent with the collapsed bridge structure. The source of the bowing distortion was not identified, but a relatively large initial imperfection was required to match the deformation under the loading conditions at the time when the photographs were taken. Incorporating the stress that caused the bowing would likely reduce the load necessary to trigger instability. The choice of the shape of the initial imperfection for the bowing distortion had an effect on the results.
figure-16-graph
Both the FHWA and SUNY/SIMULIA models were also used to evaluate the effect of corrosion in the L11 node gusset plates. The corroded condition of these gusset plates was modeled as a local thickness reduction of 0.1 inch (section loss of 20 percent) running along the top of the lower chord members. Stresses in both the U10 and L11 gusset plates exceeded the yield stress under only the dead load of the original 1967 bridge design. The models showed that the maximum stress in the gusset plates of the L11 nodes occurred in the area of corrosion at the lower end of tension diagonal U10/L11W, but that the stresses in the U10W gusset plates were substantially higher than the stresses in the corroded L11W gusset plates under the conditions at the time of the collapse. The models also predicted that the corroded L11 nodes would support much higher loads than those necessary to trigger the instability at U10W. The effects of changes in temperature at the U10 nodes were also studied with the models. Data from a weather station at the University of Minnesota showed that, on the day of the collapse, the temperature increased from a low of 73.5° F earlier in the day to 92.1° F at 6:01 p.m [NTSB 2007]. In the FHWA global model, the bearings were assumed to be fixed (but with flexibility in the piers), so that a temperature change would affect the stresses. The models showed that an increase in temperature reduced the stress in the U10 gusset plates, and thus a slightly higher applied load was required to trigger the bending instability and the lateral shift of the upper end of diagonal L9/U10W.
The FHWA investigated an additional case allowing for a difference in temperature on the east and west trusses as a result of solar radiation [NTSB 2008i]. When compared to a case with a uniform temperature change, the effects of the temperature differentials between the two trusses were minimal, with the member forces at the U10W and U10E nodes changing by less than 2 percent in the chords and diagonals and by less than 5 percent in the verticals.
Summary 
The NTSB concluded that the probable cause of the collapse was the inadequate capacity of the U10 gusset plates, which resulted from an error by the original bridge design firm, who failed to perform all of the necessary calculations to properly design the main truss gusset plates. The U10 gusset plates failed under the combined loads arising from the original bridge weight, the increases in weight caused by modifications to the bridge, along with traffic and the construction vehicles and materials staged on the bridge in an area concentrated above the U10 nodes. A review of the design showed that the U10 and L11 gusset plates were only half as thick as necessary to meet the design specifications. The finite element analysis confirmed the inadequacy of the U10 and L11 gusset plates, which were yielding under only the dead weight of the original 1967 bridge. Gusset plates that met the design specifications would have retained a significant margin of safety under the loads on the bridge on the day of the collapse.
The finite element analysis indicated that the collapse was triggered by a local bending instability in the U10W gusset plates, which occurred before any material failure or fracture. The computations also showed that the instability would have been triggered at U10W before U10E or either of the L11 nodes, even when including corrosion on the L11 gusset plates in the models. Including the bowing distortion in the U10 gusset plates that was observed in the photographs decreased the load necessary to trigger the instability, and also directed the lateral shift of the upper end of the L9/U10W diagonal to the outside of the bridge, consistent with the observations of the wreckage. Finally, the finite element analysis indicated that the temperature changes on the day of the collapse would have had a minimal effect on the load necessary to trigger the instability in the U10W gusset plates.
References 
1. Beshah, F., Wright, W., and Graybeal, B., “Mechanical Property Test Report (I-35W over the Mississippi River),” Federal Highway Administration Turner-Fairbank Highway Research Center Report, October 15, 2008.
2. Holt, R., and Hartmann, J., “Adequacy of the U10 Gusset Plate Design for the Minnesota Bridge No. 9340 (I-35W over the Mississippi River), Final Report,” Federal Highway Administration Turner-Fairbank Highway Research Center Report, October 18, 2008.
3. Ocel, J.M., and Wright, W.J., “Finite element Modeling of I-35W Bridge Collapse Final Report,” Federal Highway Administration Turner-Fairbank Highway Research Center Report, October 2008.
4. NTSB 2007, Modeling Group Study 07-115, Loads on the bridge at the time of the accident, National Transportation Safety Board, Washington, D.C., November 8, 2007.
5. NTSB 2008a, Materials Laboratory Factual Report 08-006, Hardness measurements on rivets and bolts, National Transportation Safety Board, Washington, D.C., January 18, 2008.
6. NTSB 2008b, Structural Investigation Group Chairman Factual Report 08-015, National Transportation Safety Board, Washington, D.C., March 5, 2008.
7. NTSB 2008c, Modeling Group Contractor Interim Report, National Transportation Safety Board, Washington, D.C., March 7, 2008.
8. NTSB 2008d, Materials Laboratory Factual Report 08-053, Hardness measurements on U10 and L11 gusset plates, National Transportation Safety Board, Washington, D.C., May 5, 2008.
9. NTSB 2008e, Video Study, National Transportation Safety Board, Washington, D.C., June 3, 2008.
10. NTSB 2008f, Specialist’s Study Report, Gusset plate photograph measurements, National Transportation Safety Board, Washington, D.C., July 16, 2008.
11. NTSB 2008g, Materials Laboratory Sequencing Study Report 08-032, National Transportation Safety Board, Washington, D.C., October 17, 2008.
12. NTSB 2008h, Materials Laboratory Factual Report 08-096, Laser scans and corrosion measurements of L11 gusset plates, National Transportation Safety Board, Washington, D.C., October 24, 2008.
13. NTSB 2008i, Materials Laboratory Study Report 08-118, Calculation of differential temperature for I-35W bridge, National Transportation Safety Board, Washington, D.C., November 7, 2008.
14. NTSB 2008j, Modeling Group Chairman Final Report 08-119, National Transportation Safety Board, Washington, D.C., November 12, 2008.
15. NTSB 2008k, “Collapse of I-35W Highway Bridge, Minneapolis, Minnesota August 1, 2007,” Highway Accident Report NTSB/HAR-08/03 PB2008-916203, National Transportation Safety Board, Washington, D.C., November 14, 2008.
NOTE: All of the references are available from the NTSB website. The final NTSB report in reference 15 [NTSB 2008k] is at http://www.ntsb.gov/publictn/2008/HAR0803.pdf. The other reports are at http://www.ntsb.gov/Dockets/Highway/HWY07MH024.

Complete Report on Failure Analysis of World Trade Center

Abstract
This research involves a failure analysis of the internal structural collapse that occurred in World Trade Center 5 due to fire exposure alone on September 11, 2001. It is hypothesized that the steel column-tree assembly failed during the heating phase of the fire. Abaqus/Standard was used to predict the structural performance of the assembly when exposed to the fire. Results from a finite element, thermal-stress model confirms this hypothesis, for it is concluded that the catastrophic, progressive structural collapse occurred approximately 2 hours into the fire exposure.
Keywords: 
Collapse, Coupled Analysis, Failure, Fire, Heat Transfer, Interface Friction, Structural, Thermal-Stress, World Trade Center (WTC)
1. Background 
World Trade Center 5 (WTC 5) was a nine-story building in the World Trade Center complex in New York City, NY (Figure 1). On September 11, 2001, flaming debris from the World Trade Center Tower collapses ignited fires in WTC 5. These fires burned unchecked, ultimately causing a localized interior collapse from the 8th floor to the 4th floor in the eastern section of the building (Figure 2). Debris impact was not a direct factor in this failure; the collapse was caused by fire alone.

The structural design of WTC 5 employed a common framing configuration, with steel column-tree assemblies that had beam stubs welded to the columns and cantilevering to support simple-span girders. The connections between the girders and the beam stubs were shear plates attached to the webs with bolts. The floor framing was topped with a concrete slab with welded wire fabric reinforcement.
Forensic evidence suggests that the collapse occurred during the heating phase of the fire. The columns remained straight and freestanding after the collapse (Figure 2), suggesting that the girders never developed catenary action that would have pulled columns inward, particularly as the girders cooled late in the fire. In general, the timing of this failure (early in the fire when occupants and firefighters could be in the building and therefore at great risk) is not typical for steel structures.
Exterior View of WTC
internal-collapse-area-of-WTC
2. Finite Element Analysis Approach
For this research, the nonlinear heat transfer and stress analysis capabilities of Abaqus/Standard allowed study of the mechanisms that caused WTC 5 to suffer an internal collapse. The structural plans and details of WTC 5 provided the data for an accurate model of the structural configuration.
The process involved sequentially coupled thermal-stress analyses with a heat transfer simulation to determine temperature history, followed by a stress analysis that incorporated the temperature history as part of the loading. The analyses modeled four structural bays on the 8th floor of WTC 5 (a typical bay is shown in Figure 3) using the mesh detail shown in Figure 4 for both models.
bay-framing-WTC
Structural Assembly
2.1 Heat Transfer Analysis
The model included common spray-applied mineral fiber fireproofing insulation as shown in Figure 4, in which the thermal contact between the insulation and steel, as well as the temperature-dependent properties of A36 steel, were derived from literature.
The 2005 National Institute of Standards and Technology (NIST) report on the performance of the World Trade Center Towers (WTC 1 and WTC 2) provided the basis for the effective heat of combustion and the peak heat release rate of the fire that occurred within WTC 5. The time function of the heat release rate became the input for a Consolidated Fire and Smoke Transport Model (CFAST, developed by NIST) analysis to estimate the upper gas layer temperature history of the fire.
A convective film condition on the faces of the assembly exposed to the fire environment modeled the thermal loading, using a heat transfer coefficient characteristic of turbulent, natural convective heating. Subsequently, the results of the CFAST simulation prescribed the sink temperature history of the model.
2.2 Stress Analysis
The three-dimensional temperature distribution history of the steel assembly based on the heat transfer analysis became part of the loading in the stress analysis. Other loads applied to the model included gravity to model the weight and 39 kips of pretension in each bolt to produce an idealization of the static and kinetic friction conditions at the connection.
The model utilized nonlinear, temperature-dependent stiffness and thermal expansion properties of A36 steel based on experimental data (Harmathy, 1993). Therefore, the temperature distribution history dictated the steel strength and stiffness properties. The nonlinear material properties, together with modeling to account for geometric nonlinearities, produced high-fidelity analyses of structural performance during the fire.
2.3 Failure Criterion Analysis
Forensic evidence suggests that the shear connection failures in WTC 5 were due to rupture of the web portion of the beam stems. This type of failure occurs when the bolts bear against the weak side (i.e., acting toward the free end of the member) of the bolt holes. Bearing stress of this type causes shear planes to form in the web steel. Finally, cracks along the shear planes cause catastrophic failure of the shear connection.
A simple model consisting of a single bolt and holes in connected plates provided data on the material strain condition at the point of catastrophic rupture. A failure load, derived using the AISC Steel Manual of Steel Construction (2001), applied to the single bolt model produced the required strain data. The plastic shear strain for the failure load produced the failure criterion for the full connection models.
3. Simulation Results
The temperature distribution near a shear connection after two hours of fire exposure is shown in Figure 5. In general, the average temperature of the steel agrees well with estimates from hand calculations. The results of the thermal model show that the insulation delayed the transmission of heat to the steel during the fire exposure as anticipated. Moreover, the results show that the upper region of the steel assembly remained cooler due to the heat sink effect of the overhead concrete slab.
The temperature of the beam stems at the shear connection was approximately 400 °C hotter than at the column after two hours of fire exposure. The beam stem was exposed uniformly to the hot gases and began to heat in accordance with its heat transfer properties. The cooler column (and adjacent structure) acted as a heat sink that tended to moderate the temperature rise of the beam stem immediately adjacent to the column. The shear connection was located far enough from this critical heat sink that it remained relatively unaffected, and quickly rose in temperature along with the simple-span girder.
As the steel in the compartment heated in the first hour of fire exposure, it expanded, causing the floor girder to elongate significantly and close the gap between it and the beam stem. This elongation caused relatively harmless compressive stress concentrations as the bolts pushed into the beam stem web.
As the temperature of the steel assembly increased further, the frame rigidity decreased steadily,causing the floor girders to deflect significantly. This deflection caused the lower flange of the girder to contact and deform the beam stem web, forming a fulcrum at the contact point. After about two hours of fire exposure, the loss of rigidity in the steel “outpaced” its thermal expansion, and the top bolt of the shear connection, which was pushing into the web, started to pull toward the end of the beam stem web (Figure 6).
temperature-distribution-near-shear
mises-stress-distribution
4. Discussion of Results 
According to the failure criterion derived and the results of the thermal-stress analysis, the heat-weakened shear connection experienced complete failure after approximately two hours of fire exposure. The deformation and failure of the shear connection predicted by the Abaqus model are very similar to those exhibited in failed connections in WTC 5. The angles at which the bolts pried against the bolt holes are similar in the model and the specimen (Figure 7). Moreover, photographs of failed beam stems show web deformations indicative of the fulcrum action.
comparison-abacus-forensic
5. Conclusion 
The sequentially-coupled, nonlinear thermal-stress modeling capabilities in Abaqus/Standard allowed study of the structural behaviors that led to the internal collapse of WTC 5. The analysis show that this collapse occurred approximately two hours into the heating phase of the fire after the simple span girders deflected enough to tear the connecting bolts out of the webs. It is not the precise time of failure which is aramount, but the fact that the structure failed uncharacteristically during the fire’s heating phase, rather than during the cooling phase when most fire-induced collapses occur.
The fire that caused structural collapse in WTC 5 was a severe, complete burn-out fire. As such, it is not unreasonable that the structure would experience substantial damage. However, the failure of the building to achieve the preferred performance, with the framing system surviving at least into the cooling phase of the fire, follows from the absence of analyses and design for fire exposure.
The present approach to fire protection engineering in much of the United States is primarily prescriptive, often employing propriety products to insulate structural elements and active fire suppression systems to control fire growth. Such approaches would not lead to an appreciation for vulnerabilities such as apparently existed in some of the detailing in WTC 5.
Analytical, performance-based approaches, more akin to common design for wind, seismic, and other environmental loads, are more likely to reveal critical aspects of building performance in fires, and provide engineers with the understanding they need to create designs that are robust, raise safety for occupants and firefighters, and are cost efficient.
Accurate, detailed finite element modeling can be used to assess the fire endurance of steel structures. Such simulations can be used to develop pre-engineered solutions to building codes. Additionally, knowledge of the fire endurance behavior of WTC 5 can further the understanding of firefighting risk in existing buildings of similar design.
In the case of WTC 5, relatively simple detailing changes would have enhanced the structure’s fire resistance. Slotted holes in the girder webs or increased spacing between the end of the girder stubs and the beginning of the simply supported center spans would have allowed more girder rotation without developing the prying action that tore out the girder webs. Keeping the shear connection near the face of the column would have reduced the temperature of this critical connection, thereby maintaining higher temperature-induced tear-out strengths during the fire.
In the more general case, we must acknowledge that many buildings in current use have unappreciated vulnerabilities. While analyzing and retrofitting for these vulnerabilities in existing buildings could be undertaken if justified for certain framing systems (e.g., perhaps for column-tree assemblies, if risk analyses and system testing verified heightened risk for the building system generally), finding the critical shortcomings in the present building stock would be a prohibitive exercise. However, modest expenditures of engineering effort during the design phase for new buildings can reveal fire performance weaknesses that can be avoided, often at minimal cost to construction.
6. References 
1. Manual of Steel Construction: Load and Resistance Factor Design, 3rd ed., American Institute of Steel Construction (AISC), 2001
2. Harmathy, T.Z., “Fire Safety Design and Concrete,” Longman Scientific and Technical, United Kingdom, 1993
3. World Trade Center Building Performance Study: Data Collection, Preliminary Observations, and Recommendations, Federal Emergency Management Agency (FEMA), New York, 2002